Then the motors stopped working. Tried it with motor_test.py, only got the servo action. Testing with meter, no voltage on either motor output.
At this point, I figured the driver firmware was gone. Followed your suggestion from another post and tried to download blink.
DEBUG:tornado.general:sockjs.tornado will use json module
INFO:root:Starting web server...
WARNING:root:Got message with invalid checksum
INFO:root:Read 0XACED 0.38
INFO:root:Expected 0XACED 0.38
INFO:tornado.access:200 GET /logs.html (192.168.42.20) 52.57ms
INFO:tornado.access:200 GET /js/sockjs-0.3.min.js (192.168.42.20) 44.44ms
INFO:tornado.access:200 GET /js/jquery.js (192.168.42.20) 368.43ms
WARNING:tornado.access:404 GET /favicon.ico (192.168.42.20) 24.34ms
INFO:tornado.access:200 GET /robot_control/info (192.168.42.20) 2.84ms
WARNING:tornado.access:404 GET /favicon.ico (192.168.42.20) 3.53ms
Attached is screenshot of the message
Basically, AVRDUDE not responding. It does start comms, and I do get blinking blue lights on mini.
Then I got…
Main Log
DEBUG:tornado.general:sockjs.tornado will use json module
INFO:root:Starting web server...
INFO:root:Read 0XACED 0.38
INFO:root:Expected 0XACED 0.38
INFO:tornado.access:200 GET /robot_control/info (192.168.42.20) 7.16ms
Should be good, right? Now the tilt servo stopped working. Only the camera and pan work. So it looks like a dead or dieing Duga mini board to me....
ideas?Statistics: Posted by hiropro4 — Sun May 10, 2015 12:19 am
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